Well, I got fresh gas mixed 50:1....
Still no go. Funny thing is, after draining the carb, opening he petcock, choke on, and first or second kick I could hear a little backfire in the exhaust chamber...almost like a fizz.
I just think somehow fuel is going straight from the carb into the exhaust....snuffing out the spark.
Today I kicked it about 10-12 times, pulled the exhaust off and a table spoon or two dripped out of the pipe...granted some could have been left over from me dumping it yesterday but it seems like it's loading up.
I have a new air cleaner, reeds. When I have the carb apart I can see it's clean inside. I check all the jets, shine a light to see if anything is plugged. I set the float, make sure the needle & seat didn't leak etc....
I have an blue consistent spark, new coil, stator.
Only thing bugging me is the compression is 140psi after a complete rebuild. After 10 or so kicks...not sure how many kick I should do. The guy I brought it too honed the cylinder and it still had honing marks from 8 or so years ago. Maybe I should have bored it out...or re-plated....did 87 KX 250's have plated cylinders?
?
When I get it started it runs normal....the idle does wonder up and down every now and then, nothing drastic...but it has power in 1st, kicks up the dirt.
It's a mystery..
dinky,